Progress
has been slow this past week. As some of you know I play Mr. Mom every other
weekend so I can’t get a whole lot done with the boy wandering around in the
garage. He likes to pick up small objects and randomly deposits them in various
places throughout the garage.


I did
manage to get my deep sump transmission pan installed. I picked this one up
from Summit Racing for around $40. It came with a new filter, gasket and spacer
to space the pickup down into the pan. I had originally bid on a pan from E-bay
but like many auctions there the price was bid up to within dollars of a new pan
kit yet the auctioned pan was missing the pickup spacer and filter.

Here is a shot of the new filter and pickup spacer.

Getting the old pan off was easy but once the spacer and
filter were installed there was not enough room to get the new pan in between
the valve body and cross member. I ended up having to remove the transfer
case so I could jack up the back of the transmission to make more room.


The
installed pan.


The next
chore I tackled was the disassembly of my Dana 300. It went fairly smooth until
it came time to remove the shift rails. I was working off of a few different
sets of assembly directions I had found on the internet and none of them
mentioned the rear shift rail needed to come out first. Once that was done I
ground the required notch to allow the 4:1 gears to be installed and then
cleaned and painted the case.

After work
the next day I dropped by Dennis’s shop to pull/press the new bearings and parts
onto the input and output shafts. This process took a while due to my needing
to blend installation instructions for the 32 spline input shaft, output shaft
and 4:1 kit into one plan of action.
Another
big task was finding a place to re-program the PCM to eliminate the code
relating to emissions, transmission and stock fuel tank sensor. I tried
contacting Digital Horsepower Inc. but after a few weeks of no response I
continued my search. After a brief e-mail exchange on the Pirate 4x4 forum,
Tony K from Rock Equipment pointed me in the direction of
Jim’s Performance
. I made a call and was relieved to discover Jim had done
these before and knew exactly what to do to setup the PCM for a stripped down
rock buggy. The price for the reprogramming was a reasonable $200. I also
inquired about the wiring harness and Jim said they can clean those up as well.
In exchange for $300 they will thin the harness, label the wires and send it
back with a 4 circuit fuse panel ready for installation. Since my last two
wiring attempts each took at least two weeks I jumped at this offer.

Next up on my list was the exhaust. The plan was to
mount the muffler under the passenger seat then dump the exhaust out behind the
buggy like my last setup. First I had to make some room for the muffler by
notching some of the boat side supports and then making a plate to fill in the
notched portion.

My friend Dennis had used header bends to piece together
his exhaust so I did the same. The nice thing about these is you can cut them
anywhere along the bend and still have a nice round piece that you can weld to
another bend or straight. This is a 2.50 inch diameter header bend.


Starting at the motor I attached a stock exhaust manifold
flange. This flange has an integrated flexible joint that can move in all
directions and will take up any movement between the engine and the hard mounted
exhaust system. I cut up one header bend into two pieces to get the
correct curve to get the exhaust from the manifold to the muffler.


I tried a bunch of different auto parts stores and muffler
shops but no one had any 2.50" diameter exhaust flanges. I did manage to
find a gasket at Pep Boys so I used it as a template and made my own flanges.


Another header bend was cut up to get this jog.

I'll add a downturn later.

The next big task was getting all of the controls mounted.
I also wanted to integrate a steering quikener into my steering system. The
quikener is basically a gearbox where 1 turn on one end of the shaft is
translated into 1.5 turns on the other side via a planetary gear set. The
reason for this is due to my choice of steering valve. Originally I had
4.5" stroke ram used on my previous Toyota axles. When I installed the
Dana 60's I needed an 8" of stroke ram. The old valve works but it now had
to displace more fluid to actuate the ram which translates into me having to
turn the steering wheel more to go from lock to lock (about 7 turns to be
exact). My old setup with the shorter stroke was a hair over 4 turns lock to
lock so the steering quikener should alleviate some of this extra wheel
turning..


As luck would have it the quikener fit nicely on the
steering column bracket I had used previously. This unit came from Summit Racing
and is made by Howe. I also ordered a splined coupler to connect the
quikener to the steering shaft.


With half the steering gear mocked up I wanted to get the
pedals positioned to avoid any interferences. Here is how I made the first
bracket to hold the brake pedal. I started with a paper template and then
transferred the dimensions to some 16 gauge steel. Once I had the shape cut out
with the plasma cutter I used a cut off wheel to remove a little material along
the folding lines. From there I used my hands and a hammer to get the
bracket bent.


After all that work I discovered my first bracket would not
work. I forgot to account for the master cylinders and the first bracket
had them sticking above the hood line. I was able to salvage most of my work by
making two new mounting tabs that would move the brake pedal bracket down.



I picked up the gas pedal from Summit, I suspect it is a
re-badges Lokar throttle pedal. I took a few stabs at mounting it before
settling on the position shown. basically I was trying to get it close to
the brake pedal but far enough away so I would not accidentally hit both pedals.
You can also see the steering valve which has been moved up and about 12 inches
forward from where it used to sit to make room for the coilover shocks.

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